The idea was pretty good and it actually went quite well but there were some problems and some things I just didn't like so I made a 2nd almost identical condenser...which turned out pretty much the same and I never used either of them.
In truth I've always been pretty happy with my original liebig and never really felt the need to use the new one.
So, a couple years went by and I'm cleaning things up and actually getting ready to take a bit of a break from distilling and I found a full roll of silver solder (No idea where that came from


So, I decided to go ahead and redo one of the condensers and clean it before putting it away.
So, I cut the ends off, made a new hammered flange jig out of some oak flooring and redid all but one small part of it. This actually went pretty well but at one point I was chasing leaks and my crappy propane torch, that I have to hold upside down to get to work, just couldn't handle it so I had to resort to TIG soldering, which worked just fine.
With that all finished I proceeded to start the cleaning runs. Of course the first one was water, which went fine. I steamed it for something like 3hrs. Then I added the vinegar and began steaming that.
About 2hrs into that I figured it was time to turn on the water and start condensing, which would have been followed my another water run before the sacrificial run but just before I plugged the pump in the column fell over

That's when I realized there was a slight flaw in my design...namely the fact that I used to use Easy flanges

The new design uses slip fit up to the lyne arm, then a hammered flange and try clamp to connect the condenser.
For years I've had a much shorter shotgun condenser I've used for my flute and neutral columns but it is too under powered to handle a full on stripping run.
The original version of that short condenser used an easy flange, which eventually failed and was replaced by a hammered flange, which seems to be able to handle a lot more stress.
I also usually support the big columns from the ceiling but where I was running had nowhere I could support it, so there was a fairly hefty side load going on. I thought I had made that keg connection a hammered flange years ago but I guess not.

So now I didn't get to finish my cleaning runs and will have to modify that fitting into a hammered flange fitting and maybe figure out connecting a trypod for support in the future. Not that I actually plan on doing much with it other than boxing it up and stowing it away.
This sort of thing is why I quit using easy flanges.